Jump to content
Ultimate Subaru Message Board

All Activity

This stream auto-updates

  1. Today
  2. Thanks for the advice, I'll be heading over to the shop tomorrow to drop off the replacement and I'll see if I can get a look at it or see if they've already done that themselves. When I have more info I'll update, hopefully with good news.
  3. Yesterday
  4. It's really hard to diagnose something like that without the "feel" of what it's doing that a test drive gives... Does it idle well, or does the problem happen at idle too?
  5. I know that feeling. I have an EJ turbo conversion on the go for the last four years. I’ve barely touched it in the last year. It’ll get there. Cheers Bennie
  6. Correct, the engine and wiring from the first GL swap are installed in the current Brat GL. I have a fuel pressure gauge, downstream of the filter, rigged just as you describe so it can be read when driving. 38-40 psi at idle, high 40’s when throttle opens, and holds when shut down. Actually the pressure slowly rises from 38 to 45 at engine off, holds at there for a hour, then slowly falls to zero over several hours. I think the pressure increase at engine off is heat expansion and assume the injector system is okay since it holds awhile before decreasing. The tank always pressurizes quite a bit, to the point that gas vapor smell is obvious, probably through the gas cap vent. This seems to be the only difference in the first GL with this engine and the current Brat GL-buckeroo. Your statement about the oscilloscope is helpful. It’s what I’ve been thinking is next step. (This particular model 2.2 didn’t use MAF, instead has manifold pressure sensor plus intake air temperature sensor.) I will need to get a shop to do this, but am concerned the Frankenstein aspect might add difficulty to getting that help. I’ve tried to use live data on my reader, but don’t get far. I also have back-probed at the ECU to read voltages of various sensor signal while driving, all looks solid. But the scope can show oscillations, while the meter only shows steady 12v at the injectors, for example. Thank you for the input. It’s encouraging.
  7. The L went with its owner this morning, no time to tinker so couldn’t test the mechanical advance. Haven’t heard from them so all must be well enough… Cheers Bennie
  8. Thanks! It appears someone definitely paid for the undercoating and it paid off. I've only seen some very minor flaking on the front bumper attachment points.
  9. First thought that comes to my mind is the bearing failed, the shaft got some weeble-wobble and cooked the bearing. Heat went up the shaft and cooked the rotor. If this is an optical distributor, I'd be curious of the condition of the "eye" (the little donut-shaped module that sits under the rotor beneath the metal shield.) That eye module is also made of plastic. It may have also been damaged if this is a toasty bearing scenario. :]
  10. Just realised your plates are very similar in number to my green sedan JK4474 - mine is registered as a 1989, so yours must be a very late 79 rego, and mine a very early 1980! Would be keen to see some progress pics if there's any? Cheers
  11. Man, it has been too long since the last update! Gertie is still kicking, still WOFed, and still in need of the EJ swap and certification. Life gets in the way of grand plans sometimes, but they are still in motion.
  12. MEASUREMENT METHOD For my measurement, he cams were mounted in a lathe with a 2000 point optical encoder attached to the back of the headstock. A digital indicator with micron accuracy was mounted to the carriage as rigidly as possible. The encoder and the digital indicator were then logged against time, data transfer being achieved via RS232 serial. The indicator outputs its screen reading in its own format at roughly 10Hz, and the encoder at around 50Hz in plain ASCII. Measurements were merged with respect to time after the measurement was completed. The cam was rotated as slowly as possible, approx 1.5 RPM and number of rotations were logged and averaged together to improve signal to noise. Measurements were taken with a flat face follower. This has a number of advantages: 1) The inlet cams for the EZ30D and EJ255 engines as well as all the exhaust cams run in the engine with flat faced buckets. By measurement the cam with a flat follower, you are directly measuring the valve motion. 2) Side loads on the dial indicator is minimized. This minimizes friction and deflection in the indicator. 3) The measurement is theoretically unaffected by an offset between the centreline of the indicator and the centreline of the cam. This removes one source of inaccuracy and makes setup easier and faster. The main disadvantage is that a flat follower cannot be used on a cam with concave sections, ie undercut. This is not a problem for the EZ30R cams, as viewing the reflection of a point light source against the ground surface while the cam is rotated shows that all sections of the cam are convex. The curvature of the EZ30R bucket was measured by mounting the bucket in a milling machine and dragging an indicator across the follower surface. Essentially, I constructed a makeshift gantry style Coordinate Measuring Machine (CMM). Two micron accuracy indicators were used, one for height and one for translation, for this giving XY coordinates that could be analysed. Once it was clear the curve was an arc, an arc was fitted using least squares. I did the bucket measurement a long time ago, and do not have images. THE MATHS To transform the translating flat face follower motion to that of a translating roller follower, the actual polar lobe profile needs to be calculated and then a geometric offset applied equal to the radius of the roller follower. The lift for a given angle of cam rotation is then that of a translating point follower, which is simply r – base circle diameter/2 - roller radius for any given angle of theta. I wrote quite a bit of MATLAB code to perform the data merging, measurement delay estimation, de-glitching, runout correction, and smoothing on top of this, but that is the main gist. Below is a graphical representation of the 52mm AVLS follower running on the EZ30R High lift cam at the point of maximum valve velocity. It is showing that the higher the valve velocity, the further to the edge the contact point is on the follower/bucket. I think this is why the AVLS follower is curved. Being off to the side, of the circular shaped follower, the available running area is less. The curved surface reduces the distance relative to the valve velocity. This is the best explanation of flat face follower kinematics that I’ve found to date. Props Dr Starr. This is the foundation for generating the lobe profile from the flat face follower lift coordinates http://www.me.unm.edu/~starr/teaching/me314/camprofile.pdf The dependency of the cam profile on the derivative of the lift measurement makes noise rejection / smoothing very important. Derivatives greatly amplify noise, and if too much noise is present the lobe curve begins to self intersect. Smoothing however rounds off features like the ramp transitions, so there is a balance. Obtaining low noise measurements in the first place gives the best chance of getting a clean lobe profile with an acceptably low amount of smoothing. Other considerations: 1) Run out correction. With no run out, the measurement of the base circle should be constant. If there is run out, the measurement will be a sinusoid at the frequency of once per revolution. To correct for run out, fit a sine curve,, to the measurement of the base circle and subtract it from the entire measurement. 2) The indicators have a small delay between taking a measurement and beginning a transmission of the reading, which when merged with the encoder measurement with respect to time, leads to noise in the measurement. The arduino begins transmitting the encoder reading almost instantly. By experimentally adjusting the time offset over a long measurement to minimise noise, the delay in the indicators was estimated to be around 22ms.
  13. CAM DOCTOR SHEET There have been a few cam measurement sheets and specs getting around. Like in the service manual, the duration specs seem suspiciously large. To check them, I plotted the information on a measurement sheet I found on facebook over the top of the corrected results. It appears this measurement was accurately taken with a flat face follower but not corrected for the curved shape of the AVLS follower. This exaggerates the measured duration of the cam. In reality, the EZ30R has remarkably similar cam design to the preceding EZ30D and the EJ255. Given the file extension and layout of the sheet, the measurement would have been taken on a 'Cam Doctor' machine.
  14. VELOCITY AND ACCELERATION PROFILES The measurements were detailed enough to give reasonable insight into the higher derivatives. The EZ30R cams appear use a lower peak acceleration, ie they lift off the seat slower. This could be called 'less aggressive' Peak negative acceleration is the biggest determinant for required valve spring rate, and it can be seen that all three engines are quite similar. (Actual valve spring rate is also proportional to valve mass)
  15. Knowing the EZ30R has an extra 20kW on the EZ30D in my car, I’ve always been interested in the cam specs. Especially with the AVLS system. I wasn't sure if the low lift profiles support the majority of the driving range, allowing a 'hot' high lift profile, or if there was some other strategy going on. After picking up some cams some years ago, I have finally I have had the opportunity to measure them. I also measured the cams for an EZ30D and an EJ255 WRX (2006) for a comparison. All cams are from Australian delivered models, EZ30D cams are from a junk engine I got years ago, probably 2002. The EJ255 are from a 2006 WRX with 'V25B' heads, we just happened to have some, and the EZ30R cams I have since found are 'Phase 1' or 'Pre facelift'. MEASUREMENTS Engine Cam Clearance Gross Lift Net Lift Factory Spec At 1 mm Lift At 0.050" Lift Open Close Duration At Lift Open Close Duration Open Close Duration EJ255 Inlet 0.20 9.60 9.40 5 BTDC 55 ABDC 240 0.218 -102.23 103.80 206.03 -99.93 101.25 201.18 Exhaust 0.35 9.80 9.45 55 BBDC 5 ATDC 240 0.172 -104.64 103.80 208.44 -102.28 101.36 203.64 EZ30D Inlet 0.20 9.78 9.58 5 BTDC 55 ABDC 240 0.239 -105.30 105.96 211.26 -102.99 103.50 206.49 Exhaust 0.25 9.29 9.04 52 BBDC 0 ATDC 232 0.171 -101.42 101.17 202.59 -99.10 98.79 197.89 EZ30R Inlet HL 0.43 10.12 9.69 22 BTDC 48 ABDC 250 0.255 -107.18 108.18 215.36 -104.11 104.83 208.93 Inlet LL L 0.20 3.13 2.93 N/A N/A 147 0.246 -54.07 53.72 107.79 -49.76 49.35 99.12 Inlet LL H 0.20 6.32 6.12 N/A N/A 218 0.245 -89.26 88.61 177.88 -85.55 84.65 170.20 Exhaust 0.35 9.70 9.35 60 BBDC 6 ATDC 246 0.177 -107.82 107.47 215.29 -105.44 105.03 210.47 AVLS https://commons.wikimedia.org/wiki/File:Switching_tappet_for_SUBARU_EZ30_(INA).jpg The AVLS system in the EZ30R engine is a direct acting system with an innovative concentric split follower. For each valve there are a set out outer high lift lobes and an inner low lift lobe on the cam shaft. The inner lobe runs on the inner section of the follower and the high lift lobes run on the outer section of the follower. The inner section of the fowler acts directly on the valve stem and when the system is not engaged the outer section is free to slide along the axis of the valve. When engaged, oil pressure moves a pin across that locks the outer section of the follower to the inner section and the valve then follows the high lift profile. The follower has a curved surface, with the flat axis parallel to the cam centreline. The cross section of the surface was measured to be an arc, and there is a different radius used for the inner and outer sections. The inner section was measured to have a 43mm radius and the outer section was measured to have a 52mm radius. The inner section of the follower protrudes slightly. The lobes seem like they have a slightly different base circle diameter as well. 32mm vs 32.5mm. This still leads to the high lift lobe having more clearance. During an engine build, the valve clearance is set on the low lobe, and the high lift clearance is not adjustable. To measure valve motion for the EZ30R ALVS lobes a flat follower was used and then a correction was applied to account for the curved follower. SERVICE MANUAL SPECIFIED DURATION The valve timing specifications given in the service manuals appear to be with respect to the corners of the profile ramps. The ramps end at very low lift levels and so in a practical sense, the factory open and close angles can be described as the start and end of any visible movement of the valve when viewed from above. It also roughly aligns with the peak acceleration and deceleration events. When specifying the factory specs in terms of a check lift, the non symmetrical size of the ramps makes it a little misleading. The lead-out ramp is longer that the take-up ramp. None the less, the check lift for intake cams appears to be around 0.25mm and the exhaust cams 0.17mm. The lower peak acceleration of the EZ30R cams (discussed later) seems to exaggerate the duration stated in the service manual. SPECIFICATIONS AT 1mm LIFT Aftermarket cam manufacturers tend to spec cam duration at a higher check lift, 0.050” or 1mm being common. At these levels of lift the valve has been past the ramps and through most of the acceleration phase of the profile, leaving what I'll call the bulk lift phase within the duration measurement. While the ramps and the acceleration phase can vary between cams, the bulk lift phase tends to be close to harmonic motion, which minimises required valve spring force and high frequency vibrations. SPECIFICATIONS AT 0.050" LIFT
  16. Yeah, that's one of the cleanest ones I've seen... my daily driver has enough rust that the front of the rocker moves independently of the back of the rocker if I open my door into the stop...
  17. So you tested it and found the timing does not advance with increasing engine rpm? It's probably just stuck, and needs penetrating oil and poking at until it frees up.
  18. Kinda hard to tell much from those pics... But it doesn't matter much anyway. You're going to need to inspect the distributor. Shaft wobbles so much the rotor is hitting things? Time for bushings. Some part of the advance mechanism loose and jamming into the rotor? Repair. Etc. Find nothing wrong? Put in a new rotor and inspect periodically.
  19. I'm having a hard time understanding your post. You're using the same engine and harness and ecu that you used in the rolled car, in the new car, but now it bucks? Or this is an entirely new swap? If it's all the same parts that worked before, it's obviously not incompatibilities between them or what the wiring harness supports. Or did you mismatch intakes when you originally built? Again, if it worked before, not the problem now. Since you're suspicious of the fuel supply, start with a mechanical fuel pressure gauge. Extend the hose long enough to route out through the edge of the hood and tuck under your windshield wiper. Take it for a test drive. Fuel pressure should be solid, and should go up 12 psi when you go from idle to full throttle. Does it buck at idle, or only above a certain amount of engine load? On your obdii scanner, use the live data mode (if it doesn't have live data, bin it and spend $50 on a new one), looking for any sensors that move in a sudden fashion, especially if it correlates with the bucking. If it's a fuel injection issue, an oscilloscope is really handy... Here's a couple pics from last time I was troubleshooting a bucking issue: https://imgur.com/a/RwWTdwG In these images, the jumpy green trace confirmed the bad component - MAF sensor.
  20. Hi All, I’ve been learning from this wonderful site for half-dozen years, so let me start my first post with a hand-clapping thanks to the many people who’ve helped me along. I bought an ‘83 GL new, kept it all these years, and in 2021, swapped in a 2000 Impreza 2.2, California spec. My fun with that wagon ended with a roll-over, last year. I’m lucky to have found a running Brat (1985) and began pulling over the parts from the wagon, which included the 15” wheels and 2.2 fuel injected engine, wiring harness, and pretty much all the interior fittings. Now to the point of this post. I am unable to make the engine run in the Brat as it did in the wagon. The engine starts, idles smoothly, and can have full power. But intermittently. The stutter/cut-out is throughout the whole range of throttle, and depending on the rpm, can best be called ‘bucking’. The fuel system in the donor car had an in-tank pump with sensors for fuel level, pressure, temperature, and control valves for drain and purge (not the purge valve at the fuel rail). None of the sensors and valves came over to the Old Gen cars, although I did preserve the sensor wires to the area of the ECU. I ran a 5/16” line from an external Ford fuel pump to supply the engine, and used the original 1/4” supply as a return, and the 3/16” as a vapor line from engine to tank. That worked fine on the wagon, but I suspect the current problem is related to this set-up. I’ve replaced a lot of the sensors: front O2 at the exhaust, knock, throttle position, engine block temp, crank sensor, and tested the purge control valve to be operational with voltage, also the ECU with another. Also new plugs when moving the engine to the Brat, and then a new coil. The plug wires were new 5,000 miles ago, so don’t think the problem is in the ignition. I realize this is a vague description of what is in place right now, and hope someone will be interested and start a conversation to help with the next step. I’m wondering if anyone has opinion/experience with the Cali-spec engine and whether my wiring loom can support an older (Gen1) intake and its ECU. I’m feeling pretty desperate and leaning toward finding a mechanic willing to work on this swapped set-up, with the thought that a more sophisticated diagnosing kit could narrow down the issue, whether the ignition or fuel is quitting. I’m working with a simple OBD reader, multimeter, pin-out chart for the ECU, and a 72- year old brain. It’s tough. Thanks for your time.
  21. Hey bushytails, Thanks for that mini procedure for an easy check of the mechanical/centrifugal advance. I might have a tinker if I get the chance before it disappears. I don’t think the fuel mixture is rich as I changed the carb due to an idle issue. The replacement stock hitachi was known to run well and I haven’t seen anything different than expected. No black smoke indicating running a rich mixture and no running on that’s common with a rich mixture and engine shut down. Thanks for all of your thoughts on this. I think it can safely be put down to an issue with the mechanical/centrifugal advance. It’s interesting that it runs so well with static timing set at 20° BTDC. Cheers Bennie
  22. Last week
  23. Howdy all, I have my 88 GL in the shop getting its engine resealed. I got an update from them an apparently the distributor rotor had melted in the distributor, or potentially tore it somehow? It wasn't melted/torn at the head, but at the base of the rotor head. Luckily it turns out I have an extra, however would anyone know why something like this would have happened? It was an older part, and I don't when it was last replaced, so it could be that it was just on the way out anyways. I hadn't had any issues with anything ignition or engine electrical before. I'm a bit worried that they're going to put the replacement in and the same thing might happen, it not immediately, maybe a few 100 miles down the freeway. Attached are some photos of the damage the shop sent to me. Any wisdom would be appreciated. Thank you! -Philly
  24. From what I can see, that car looks surprisingly solid. Nice find!
  25. Have you taken this thing to a muffler shop and let them take a look at it? They’re probably going to be in the position to tell you what’s going on.
  26. First post! Here are some pics of my 88' GL. I call her Constance. I have just about a million photos of her, but these are some of my favorites. Everything is stock except the exhaust which custom made by the last owner, nothing loud just not stock. Not exactly sure why it was done but it's not an issue, so I don't mind. Also, the rims were painted black which I'm a huge fan of. -Philly
  27. Oh wow, didn't foresee that issue with brake-to-strut clearance! Would be interested to see another angle of that.
  28. Yes, the weights and such are the mechanical advance. With the vacuum advance disconnected, slowly rev the engine up. The timing should advance proportional to engine rpm, to about 3000rpm or so. I don't have an advance curve for the ea82 handy, but it should just smoothly increase with rpm until it reaches a limit around 2-3k. Another possibility is your mixture is way rich, and you're hiding it with timing. Overly rich mixtures burn slower and need some extra timing to compensate.
  1. Load more activity
×
×
  • Create New...